Sweeney
NES Member
...but not intended.
My matched G98 has a broken stock. It broke at the weakest point where there is little wood.
I glued it once with Gorilla Glue but after a few shots it came apart due to the integrity of the wood.
It is now undergoing surgery after mulling it over and devising a plan. I settle on boring out the mating ends of the stock and fitting a dowel. I'll be using Acra 20 epoxy for bonding.
The first order of business was to get the holes in the right position and attitude. I centered the holes on the bore for the cleaning rod, clamping the stock bits to the table of my Bridgeport. A 6mm socket head cap screw was used in the cleaning rod bore to center the victim... um... patient.
A right angle plate took care of alignment front to back. I ran an indicator down the sides of the barrel channel to align side to side.
I used a 0.625" end mill to bore the holes. This size would not perforate the exterior and the dowel is just big enough to accommodate the cleaning rod nut leaving about 0.125" of material on the sides and top.
When done the repair will be invisible as the 'seam' is hidden under the band. Once epoxied I'll mill the mortise for the cleaning rod nut then see how it holds up.
My matched G98 has a broken stock. It broke at the weakest point where there is little wood.
I glued it once with Gorilla Glue but after a few shots it came apart due to the integrity of the wood.
It is now undergoing surgery after mulling it over and devising a plan. I settle on boring out the mating ends of the stock and fitting a dowel. I'll be using Acra 20 epoxy for bonding.
The first order of business was to get the holes in the right position and attitude. I centered the holes on the bore for the cleaning rod, clamping the stock bits to the table of my Bridgeport. A 6mm socket head cap screw was used in the cleaning rod bore to center the victim... um... patient.
A right angle plate took care of alignment front to back. I ran an indicator down the sides of the barrel channel to align side to side.
I used a 0.625" end mill to bore the holes. This size would not perforate the exterior and the dowel is just big enough to accommodate the cleaning rod nut leaving about 0.125" of material on the sides and top.
When done the repair will be invisible as the 'seam' is hidden under the band. Once epoxied I'll mill the mortise for the cleaning rod nut then see how it holds up.
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